Cowan rail accident | |
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Details | |
Date | 6 May 1990 |
Time | 7:20 pm |
Location | Brooklyn, New South Wales |
Country | Australia |
Rail line | Newcastle and Central Coast railway line |
Operator | 3801 Limited, CityRail |
Type of incident | Collision |
Cause | Signaling fault |
Statistics | |
Trains | 2 |
Deaths | 6 |
Injuries | 99 |
The Cowan rail accident occurred at 7:20pm on 6 May 1990 when the 3801 Limited special steam passenger train returning from the Morpeth Jazz Festival was struck in the rear by the following CityRail inter-urban passenger service. The steam train had stalled while attempting to climb the steep gradient from the Hawkesbury River to Cowan, New South Wales, and it was found that sand applied to the rails to regain traction had interfered with the signals and given the following train a false clear indication.
Contents |
The crash occurred approximately 5 kilometres (3.1 mi) south of Brooklyn, New South Wales, near the Boronia No. 3 tunnel. The railway line at this point, known as the Cowan Bank, is 2.5% (1 in 40) grade and, as the special hauled by C38-class steam locomotive 3801 passed southwards through the No. 3 tunnel, the wheels of the locomotive started to slip. The driver of 3801 applied sand to the rails to improve traction, but the train came to a complete stop approximately 50m clear of the tunnel. Passengers on the steam train reported seeing a signal fluctuating aspects between green and yellow. The following CityRail V set inter-urban train, which had been halted at the northern entrance to Boronia No. 4 tunnel for 10 minutes by a red stop signal, received a green indication and proceeded, colliding with the steam train shortly after.
The impact killed the driver of the inter-urban, Gordon Hill, and a passenger who was riding in the inter-urban's cab, as well as four passengers in the rear carriage of 3801's train. 99 passengers were injured, 11 of those seriously. The force of the crash completely destroyed the last carriage of the steam train, and was enough to break the locomotive coupling and push the engine 12 meters forward.
A coronial inquiry heard by Mr Derrick Hand subsequently found in December 1990 that the sand that had been applied to the rails by 3801 to aid traction had insulated the train from the rails and had caused the track circuits to fail to detect the presence of the train in the block, allowing the following inter-urban train to be given a false green clear aspect (known as a Wrong-side failure). Mr Hand also considered it likely that a passenger on 3801 had applied a handbrake on the third carriage, and that this, combined with the heavy load, steep grade and curvature of the line had prevented the steam train from restarting. No fault was found with the signalling system, although the coroner recommended that it be upgraded as soon as possible.
Contributing factors include:
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